Volume Control did not exist, It was ignored. This is the ultimate reason the Horizon allowed 1000 Bbls of hydrocarbons to enter the well. It is common training to ensure we recognise gains of 10-20 Bbls and react by shutting in the well. It is not the Co Man, TP or OIM who sanction this decision. It is the trained action of a good Driller and Logger working together. 1000 Bbls is too late! Too late to decorate the story with other faults. Other ‘faults’ occur in [U][B]all[/B][/U] wells, but the trained actions of drill crew are there to prevent escalation and recognise the anomalies.
I recognise that many of you on this site have never been on a rig or understand the complex systems employed, but I’m making a big effort to offer impartial knowledge. In our industry, it is known among drilling crews that components in the well fail and that we are trained to intervene. And, we will intervene. [B]How would we have intervened in the case of the Macondo if volumes were being monitored? I guarantee you that the well would have taken in a maximum of 20 Bbls of hydrocarbons if systems had been in place to monitor volumes. Hopefully, one of you guys advertises this fact to the realists in the industry! Guaranteed[/B]!
Bottom line: Volume control did not exist…and anything could happen! That ‘anything’ did happen!
And remember, the investigative team have absolutely no knowledge of the oilfield industry. And yet, their conclusions are considered ‘sound’.
Like I’ve said before, the guilty are Vidrine, Kaluza, OIM, Night TP (and Day TP who passed on info on how to proceed!!!), and the Driller, the people deciding the results of the Negative test. The Guilty concerning the volume control-less blowout are the Driller, the TP, the Swaco mud engineers and ultimately the OIM and Day TP.
Ignoring volume control is the reason why this whole fiasco is being considered by Joe Public, the reason armchair engineers think they understand better than the industry, the reason for rocket scientists in Universities to offer their thoughts on the subject.
All Blowouts are preventable with crews who understand the importance of pressure and volume control…and it doesn’t matter what fails in the well! Naturally, a working BOP is handy!
The big question to ask is: am I wrong? Is this arrogant son of a B wrong? Or, is the investigation simply a stage, a play, a place to smooth over the politics involved with finding an appropriate fall guy. I say trust the BP and Marathon reports. They have too much to lose if proved wrong!
And what of the other Operators who were questioned by the commission? Guaranteed, they enjoyed watching BP swim without realising their futures were also affected by the demise of the Macondo well. All this crap about “we wouldn’t have done this” is complete crap. They have all been in the shithouse but for intervention by good crews.
One final thought!..Why are BP so quiet about this considering the adverse publicity? Why not act earlier? Why not stand up for their CEO for so long? And why let him go? Why have they not fought this according to my forthright opinions? Obviously, the company is bigger than any ‘fall guy’, so they took the opportunity to alleviate some of the pressure hanging around their necks, and we all know the source of that uninformed pressure, by sacking the CEO.
Now, Justice is something we all crave, but appeasement will be the only result! There’s too much politics and too many other fall guys concerned. An escalation of this battle will only result in adverse publicity to the GOM drilling activity and you can be sure there will be privacy and closed doors on the official legal investigation to ensure no further widespread public agitation occurs. Armchair engineers!