The agreement also sheds additional light on communications between Deenadayalan and Radhakrishnan Karthik Nair, a Synergy technical superintendent who was indicted last month alongside two ship management companies.
According to the filing, Deenadayalan admitted that Nair directed him to send a “convincing” email to the vessel’s charterer regarding the Dali‘s fuel consumption to avoid drawing attention to the use of the flushing pump.
More that Federal prosecutors, I think the one who have reached a deferred prosecution agreement is the chief engineer and this may give him the chance to reduce final punishments, but hazard to the safe navigation of the vessels and endanger bridges, structures and shore facilities is the full lack of risk assessment of old design conception of this infrastructure, and inadequacy to today’s ship dimensions, speed, etc. from shore institutions, port authorities, coast guard watch, etc.
Technical superintendent and ship management companies are the most weak shackle in the chain not covered by failing to due diligence, where the crew is covered.
The 2 paragraphs below from the gCaptain article were the most puzzling to me. I’ve heard proper names of equipment butchered all kinds of ways depending on the type of vessel, country & even what body of water ships sailed on. I had to use A.I & research to ensure I knew what the NTSB was talking about with the term, “flushing” pump. When this incident happened none of the professional mariners on this forum were in the ballpark concerning the cause if the NTSB is pinning it on modified fuel pumps on the generators. From what I read those guys on the Dali had a really weird set up. I’m not sure I completely understand it still.
From the gCaptain article:
“At the center of the case is the flushing pump, which prosecutors say was improperly used to supply fuel to two diesel generators despite not being designed to automatically restart after a blackout. As a result, the generators allegedly lost fuel supply following the first outage, leading to a second blackout that left the vessel without propulsion or steering moments before impact.”
“Separately, shipbuilder HD Hyundai Heavy Industries has alleged that the vessel’s operators bypassed built-in redundancies after delivery by replacing automatic fuel supply pumps with the non-redundant flushing pump, a modification the company said violated classification rules and contributed directly to the second blackout.”
In the report it says that neither of the CEs interviewed knew how long the flushing pump was being used instead of the circ/supply pumps. This could easily be determined by the flow meter in that loop. If hours on GEs 3 and 4 are increasing but the flow meter reading is not increasing, then they are on the flushing pump. (Assumes meter is not bypassed)
gCaptain article says both federal prosecutors and the builders yard claim there were illegal modifications made. The problem is not the modifications (which were surely class approved as part of the exhaust gas scrubber installation) but rather how they were operating the plant. Using the flushing pump (no standby pump, no auto restart feature) as a normal lineup ESPECIALLY during maneuvering is inexcusable.
Based on the lineup in use at the time of the blackout (page 92), once the ME circ/supply pumps restarted, GEs 1 and 2 should have been available. I realize the recurring electrical fault made this moot, but just curious why all the focus is on DGs 3 and 4 being unavailable as if those were the only available DGs.
A sudden stoppage of the fuel supply would explain why both generators would shut down at the same time, as they share a common fuel line, and also prevent the standby generator from starting automatically. But since the ship was presumably using LSMGO, they might have been using the small flushing pump instead of the dedicated fuel oil booster pumps for the generators.
So emissions control complicated the system so much that the designed system could not be used for fear of prosecution from the eco idiots so the Dali used a work around that failed under stress.
Good job eco idiots
No air pollution
Just 6 dead brown people so no big loss there
A few more brown people still stuck in Baltimore ( allegedly a worse place than Islamabad)