Deepwater Horizon - Transocean Oil Rig Fire

News to me…FYI from theoildrum.com by ResevoirGuy 5-31-10


On at least three occasions, BP records indicate, the blowout preventer was leaking fluid, which the manufacturer of the device has said limits its ability to operate properly.

“The most important thing at a time like this is to stop everything and get the operation under control,” said Greg McCormack, director of the Petroleum Extension Service at the University of Texas in Austin, offering his assessment about the documents.

He added that he was surprised that regulators and company officials did not commence a review of whether drilling should continue after the well was brought under control.

After informing regulators of their struggles, company officials asked for permission to delay their federally mandated test of the blowout preventer, which is supposed to occur every two weeks, until the problems were resolved, BP documents say.

At first, the minerals agency declined.
“Sorry, we cannot grant a departure on the BOP test further than when you get the well under control,” wrote Frank Patton, a minerals agency official. But BP officials pressed harder, citing “major concerns” about doing the test the next day. And by 10:58 p.m., David Trocquet, another MMS official, acquiesced.
“After further consideration,” Trocquet wrote, “an extension is approved to delay the BOP test until the lower cement plug is set.”

When the blowout preventer was eventually tested again, it was tested at a lower pressure — 6,500 pounds per square inch — than the 10,000-pounds-per-square-inch tests used on the device before the delay. It tested at this lower pressure until the explosion.